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MkIII was designed using a CAD package to get the dimensions more
accurate. It worked in a was in that the entire chassis and side
armour were made out of one piece of polycarbonate, and it would
have been difficult to work it all out on paper.
The problems with this design were that the flipper was too far
forwards, and the only way to get it to self-right was to add a
huge M2 rod attached to the front of the flipper that reached all
the way to the back of the robot.
MkIII is imminent.
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